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Description
These are my configs for a out of the box tinymovr:
When i now try setting the tm in velocity mode, calibration or position mode , it draws a very high current spike , and then doesnt end up changing its mode. This particular tinymovr was working for sometime under similar params before as well, until once when it kept drawing a lot of current and ended up burning a really costly motor. At the instance it was powered by a 6s 24V battery through a PDB. Now im trying to test it using a dc regulated power supply which limits current if it exceeds the limit. Why is this happening and whats the fix for it?
The specs are:
Tinymovr R5.2 with out of the box firmware and studio 1.6.5
Maxon Motors EN-21-306
params are stated in the datasheet have been put in as configs here
I feel theres an internal problem with the tm in which case i want to first rule out other possibilities and then look for replacement.
